With the Company, the main pollution sources from the production process are: dust, wastewater containing chemicals, solid wastes, air emissions and organic solvent. Wastewater from the factory is 3,000 m3/year containing chemicals from cooking process and bleaching process such as: H2O2, NaOH, SiO2, diesel fuel without any treatment and 80kg solid wastes (rattan, rattan cover). Besides, the exhaust fumes and dust which are frequently emitted to the environment, has affected adversely the workers’ health and surrounding environment.
Perceiving the importance of applying CP to improve production performance and solve environmental issues, the Company has actively participated in the CP demonstration project of the Cleaner Production in Industry Component since 2007
The Company has set up a CP team, including 10 members, to review and identify obstacles and analyze solutions to save energy and resources. The Team has cooperated with CP expert to focus the assessment on the primary process of rattan and finishing process of product.
Consequently, the team has proposed 27 CP solutions for application. Some of those were applied and brought the following benefits.
Typical Cleaner Production options of the Company are as follows:
Remarks: GH: Good Housekeeping;
Together with Cleaner Production option, the Company also invested in replacing the old rattan bleaching system by the new one with heating process. Previously, the factory had 7 bleaching tanks (including grey bleaching and white bleaching) with capacity of 3 m3 each tank, 130 kg of rattan each batch. Because they use lots of chemicals and process in normal temperature, the bleaching time is long (about 30 hours). Besides, the tanks are made from cement so they are quickly eroded causing leakage with chemicals. Installing stainless steel tank can lengthen lifetime of tank. Combining with heating process can increase bleaching efficiency, reduce chemicals consumption and bleaching time. The bleaching test results showed that chemicals consumption can be reduced by 40%, water 40%, bleaching time 50%. It was estimated that when the line come into operation, the Company could save up VND 30 mils of production cost monthly. Currently, the Company also invests in building rattan drying system and wastewater treatment system.
Investing in CP has helped the Company ensures the sustainable development and production, increase the prestige of the company with domestic and overseas partners, especially in the context of economic accession when quality, management and social responsibility criteria are higher and higher.
By SCP